From the ChibiOS HAL I2C driver pages:
After a timeout the driver must be stopped and restarted because the bus is in
an uncertain state.
This commit does that stopping explicitly on any error that occurred, not only
timeouts. As all the i2c functions restart the peripheral if necessary it is
safe to do so.
Co-authored-by: Dasky <32983009+daskygit@users.noreply.github.com>
Co-authored-by: Dasky <32983009+daskygit@users.noreply.github.com>
* Use polled waiting on platforms that support it
Due to context switching overhead waiting a very short amount of time on
a sleeping thread is often not accurate and in fact not usable for timing
critical usage i.e. in a driver. Thus we use polled waiting for ranges
in the us range on platforms that support it instead. The fallback is
the thread sleeping mechanism.
This includes:
* ARM platforms with CYCCNT register (ARMv7, ARMv8) this is
incremented at CPU clock frequency
* GD32VF103 RISC-V port with CSR_MCYCLE register this is incremented at
CPU clock frequency
* RP2040 ARMv6 port which uses the integrated timer peripheral which is
incremented with a fixed 1MHz frequency
* Use wait_us() instead of chSysPolledDelayX
...as it is powered by busy waiting now.
* Add chibios waiting methods test bench
* Disable RESET keycode because of naming conflicts
* Add Pico SDK as submodule
* Add RP2040 build support to QMK
* Adjust USB endpoint structs for RP2040
* Add RP2040 bootloader and double-tap reset routine
* Add generic and pro micro RP2040 boards
* Add RP2040 onekey keyboard
* Add WS2812 PIO DMA enabled driver and documentation
Supports regular and open-drain output configuration. RP2040 GPIOs are
sadly not 5V tolerant, so this is a bit use-less or needs extra hardware
or you take the risk to fry your hardware.
* Adjust SIO Driver for RP2040
* Adjust I2C Driver for RP2040
* Adjust SPI Driver for RP2040
* Add PIO serial driver and documentation
* Add general RP2040 documentation
* Apply suggestions from code review
Co-authored-by: Nick Brassel <nick@tzarc.org>
Co-authored-by: Nick Brassel <nick@tzarc.org>
* Add ifndef to WS2812 timing constraints
Due to the way that the PrimeKB Meridian PCB was designed, this change
is needed in order to properly adjust the LEDs.
Testing:
* Compiled primekb/meridian:default successfully
* Compiled random board (walletburner/neuron:default) successfully
* Fix linting errors
Missed some spacing
* More linting fixes
Spacing on the comments... really?
* Rename WS2812 timing parameters for clarity; add comments
* Add docs update for the WS2812 timing macros
* Fix typo on comment
* Add ifndef for WS2812_RES
* Update double backticks and table with parameters
* Move timing adjustments documentation to ws2812_drivers
* Move timings adjustment discussion to bitbang section
* Update T0H and T1H definitions in subtractions
* format
Co-authored-by: Gondolindrim <alvaro.volpato@usp.br>
Co-authored-by: zvecr <git@zvecr.com>
* Add support for RISC-V builds and GD32VF103 MCU
* Add toolchain selection in chibios.mk based on the mcu selected in
mcu_selection.mk
* Reorder and added comments to chibios.mk to have a streamlined makefile
* Add GD32VF103 mcu to possible targets for QMK.
* Add STM32 compatibility for GD32VF103 MCU, this is hacky but more efficent
then rewriting every driver.
* Add GigaDevice DFU bootloader as flash target, please note that
dfu-util of at least version 0.10 is needed.
* Add analog driver compatibility
* Add apa102 bitbang driver compatibility
* Add ws2812 bitbang driver compatibility
* Add eeprom in flash emulation compatibility
* Allow faster re-builds with ccache
* Add SiPeed Longan Nano to platform files
* Add SiPeed Longan Nano Onekeys
* Make quine compatible with other bootloaders
* Support builds with picolibc
* Add risc-v toolchain to arch and debian/ubuntu scripts
* Move Audio drivers from quantum to platform drivers folder
* fix path for audio drivers
Co-authored-by: Ryan <fauxpark@gmail.com>
Co-authored-by: Ryan <fauxpark@gmail.com>
* Add RGBW support to PWM and SPI drivers for ChibiOS
* Apply suggestions from code review
Co-authored-by: Ryan <fauxpark@gmail.com>
Co-authored-by: Ryan <fauxpark@gmail.com>
* Align ChibiOS I2C defs with other drivers
* Update keyboards/xelus/valor_frl_tkl/config.h
Co-authored-by: Ryan <fauxpark@gmail.com>
Co-authored-by: Ryan <fauxpark@gmail.com>
* Make solo half of split keyboards (more) usable.
Using only one half of a split keyboard (that's using the split_common
framework to communicate) is not a great experience, since several read
timeouts per scan cycle cause an unusably slow scan rate.
This change blocks all split communication attempts for 500 ms
(configurable) after an error occurs, causing the scan rate to become at
least _more_ usable, but might need some tweaking to work fully on most
keyboards. One read timeout still needs to occur after the 500 ms has
passed, and if that timeout isn't low enough, some scan cycles may still
be too slow.
* Fix lint complaint.
* Require 25 consecutive comm errors to see comms as disconnected.
The number of max errors can be overridden by defining
`SPLIT_MAX_CONNECTION_ERRORS`.
* Add comments to new defines, and ability to disable disconnection check.
Also increase `SPLIT_MAX_CONNECTION_ERRORS` to 40, since it's divisible
by most relevant numbers for the description.
* Make lint happy ...again
* Only update `connection_check_timer` when needed.
* Add new defines to split keyboard documentation.
* Move connection timeout logic to transport.c, add `is_transport_connected`.
* Use split_common disconnection logic in matrix.c.
Instead of doing more or less the same thing twice.
* Move disconnection logic to `transport_master`.
Is a cleaner implementation, and causes the scan rate while disconnected
to increase instead of decrease.
* Lint fixes.
* Lower default `SERIAL_USART_TIMEOUT` to 20 ms.
The read timeout must be low enough to not cause exessively long scan
cycles when using a solo split half. 10 ms was determined from testing
to work fine even with the slowest defined baudrate of 19200 (5 ms was
too low for that case), so 20 ms should be fine for most cases.
* Remove `SERIAL_USART_TIMEOUT` from ergodox_infinity/config.h
Was somewhat mistakenly included in an earlier PR.
* Fix building with `USE_I2C`.
* Reduce built firmware size.
Not really sure why this works, the idea was taken from tzarc's work on
split disconnection.
* Tweak and improve opt-out for split disconnection logic.
There are now two ways to opt out from this feature:
* Set `SPLIT_MAX_CONNECTION_ERRORS` to 0. This will completely disable
the connection status checks (also affects the slave matrix reset logic in
matrix.c, though).
* Set `SPLIT_CONNECTION_CHECK_TIMEOUT` to 0. This will only disable the
communication throttling while disconnected. Will make the firmware
smaller.
* Make split disconnection logic work with custom transports.
Includes a fallback implementation for keyboards using a custom
split_util.c but not a custom matrix.c (currently no such keyboard seems
to be merged, though).
* Remove unnecessary include of timer.h
Co-authored-by: Joel Challis <git@zvecr.com>
Co-authored-by: Joel Challis <git@zvecr.com>